The front left motor on my HubSan Q4 stopped working recently, so I bought some new motors and replaced the broken one. This is a step by step guide to how I accomplished the repair.
In order to make the repair, you need a soldering iron and solder, a screwdriver, tweezers, and pack of new motors. A small pin vice might also be useful, but fingers can work just as well.
Remove the propeller by pulling it gently upwards. They usually come off fairly easily. If it doesn’t then use a soft plastic (or balsa?) implement as a lever between the top of the motor and the base of the prop hub.
Next, carefully release the motor.
And push the two white mounting clips inwards to release the white plastic motor mount from the PCB. This leaves the motor free, apart from the two soldered power wires. This is done after lifting the motor upwards and out, otherwise there isn’t enough room for the clips to move in and clear the PCB.
Next, desolder the two motor wires, noting that white is (+) and black is (-), although it’s identical to the other motor. Don’t use too much heat, it should only require an instant to release the wire. This is where the reason for removing the white plastic motor mount first becomes apparent. It’s too close to the solder pads to avoid melting it with the soldering iron otherwise. The picture below went a bit wrong as I accidentally clicked the motor back into place when I put it on the desk to take the picture. Just pretend the motor is hanging through the hole as in the previous shot.
Remove the old motor completely and mark it as defective so it won’t get confused with any of the new ones. Select the correct type of new motor from the pack. In this case it’s the black and white wire motor, not the red and blue one.
Insert the new motor into the plastic mount, making sure to get the wires coming out of the correct side and from the right hole. This is what the tweezers are for, as it’s a very fiddly operation.
Now solder the new motor in place. The pictures with the soldering iron are actually posed for the camera. There are two reasons for this: firstly, I don’t solder on a piece of white cardboard and, secondly, I only have two hands. The soldering iron is cold in the photos and propped up precariously on its stand with me holding the tweezers. The pictures show the motor, NOT clicked into position, but held by its powerful magnets against the metal pin vice. This will work well, but I found it just as easy to hold the job with my fingers and solder it that way. Obviously, not burning your fingers is the most important point if you choose to hold it, so only do this if you are confident with a soldering iron and do it every day. If you press the wire down against the PCB so that the exposed part sits on the solder connection, then you can just about get away with it without burning yourself. Otherwise, use the tweezers to press the wire against the PCB and use as little heat as possible. A little solder run onto the wires and pads always helps.
When soldering the wires, make sure to get the direction of wire entry to the solder pad correct. This will aid with tidying up the wiring afterwards and make sure it doesn’t catch on anything. They both point inwards like in the picture.
At this point I like to test that the electrical connections are all good and that it all works as expected. In order to see the motor spin, I’ve attached a piece of tape to the spindle.
That’s almost it, but you have to release the motor from the plastic mount as if you were going to take it out, then push the white mount fully into the PCB before replacing the motor. The reason for this is that there isn’t enough clearance for the mount to go into the PCB with the motor taking up all the space inside. Also, note in the picture two small plastic lugs which must be carefully located into a cut-out in the circular PCB hole. If you look at the circular hole carefully, you can just see the cut-out to the left of the “B” where the two wires are disappearing underneath.
Release the motor to make space to click the mount in.
Now push the white motor mount downwards to click it fully into place. The white plastic is quite brittle, so it’s important not to use too much force. Slip the motor to one side before pushing down so that it reduces the stress and the lever effect as the clips go in. Otherwise you can crack the mount. In other words, make sure the motor isn’t pushing the top lugs outwards when you push the mount down into place.
Finally, push the motor back into place and fit the propeller.
And we’re ready to go flying again!
Everything works and it lifts up into the air again. I’ve never managed to film myself flying it yet, because every time I try and get the quadcopter into the camera’s view I lose control and crash into something.
Also, don’t forget that the trim is likely be a long way out after changing the motor, so you might want to do a trim reset first on a level surface. Mine was drifting back and right quite a lot, but I was just happy to be flying it around again. I have a knack for finding the neutral operating point after years of test flying other people’s models and have a habit of just flying models the way they are. I’m not sure if that’s a strength or a weakness, but I have had a few occasions where I’ve flown a model seemingly perfectly, then, when somebody else flew it after me, they nearly crashed. There was that electric glider that went vertical immediately after launch which was a bit of a shock for the pilot, but I probably shouldn’t mention that.