Well, true to my word, I repaired the autogyro back to flight ready status in a week. Unfortunately, the weather conspired against me. We had violent electrical storms the night before and forecasts of storms the next morning. Although it did rain quite hard, I’m not sure that the storms every really developed, but one place I don’t want to be is standing in the middle of a field holding a radio transmitter when there’s electrical activity overhead.
As for the repair, I stuck the spruce longerons back together again.
Then the fuselage sides got glued back together where the LiPo had moved forwards in the crash and separated them. You can just see in the picture below that I’ve also had to add a plywood plate where the spruce longerons meet the red fuselage. It’s just visible on the right of the picture and, if you compare to the area with the sellotape in the picture above, you should be able to make out the new 2mm plywood strengthening plates.
I’m a bit worried about making this area too strong, as it will eventually just break at the point where the spruce meets the fuselage. After that, I’ll be trying to dig the longerons out of the fuselage to replace them as they extend right up to the rear former.
Apart from sticking Pete the pilot’s head back on, the only thing left was the motor.
I probably could have bought a replacement shaft for the motor, but I chose to make my own out of a piece of 3.2mm rod.
You can see my new motor shaft at the bottom of the picture. It’s not quite perfect like the machined original above, but I made it and I like it better. Actually, it made me wonder what the commercial motor shafts are made from, as the original was obviously designed to fail rather than bend the motor bell in an impact. That didn’t exactly work and a shaft costs £3 while a brand new motor costs £10. My solid steel shaft is a lot stronger than the original, so one more hit on the ground like before and it’s going to be a new motor. I can live with that.
So there we are, one fixed autogryo and I’ve now got a whole week to properly test that everything works before committing it to the air again. Next time out I’m going to increase the shim under the rear of the blades to 0.8mm, which should reduce the lift and help with the launch.
That’s it for this week, but I did video the autogyro’s reconstruction last night, so I might post that later depending on how it came out. Let’s hope the conditions next week are more conducive to autogyroing.